Thursday, November 8, 2007
Prep Session #2
I tested ut the arm I made last session and it didn't work because it was too heavy to be controlled by the hand held controllers so I tryed to connect it to the main robot, and that didn't work either. So for the rest of the session I built diffeent parts of arms to find out how I could make an arm that was long enough and light enough/strong enough at the ame time.
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